What a great day, I have the engine running at last and we’ve been able to sit outside in the sun for the first time this year!
With hindsight I should have mentioned the following yesterday, I had intended to but as part of what I hoped would have been a successful trial of the engine then, had I done so regardless I suspect someone would have pointed out a possible problem, especially as I was going to upload a photo of what I had done…
Bear in mind that I have never owned or used a compressor before – when it arrived the screw in air filter was smashed in the box, I had emailed the supplier and had an immediate response saying they would ship another filter straight away, great, can’t ask for more than that of course, so I forgot about it and as a make do to try the engine for a short period I placed the foam filter material loose in front of the air intake with a rubber band. The compressor backfired / misfired twice when I was using it and blew the top off the engine oil cover… I was so concerned in trying to get the engine to run I paid no attention – sorry, I can hear the groans. Anyways I got to thinking about this for some reason early hours this morning and I was remembering Neil saying about how it may not have enough air to get around DC – it slowly dawned on me, off I went to check and sure enough the foam had been sucked down the inlet pipe and was all compressed in there effectively blocking it. So to cut the story short with the foam removed the compressor ran for much longer before auto cutting off and filling the air tank and the pressure level at about 10 bar I think, it was barely on the scale yesterday – this together with the flywheel now spinning with the crankshaft the engine couldn’t wait to get going – and it seems to run very nicely now!
The broken Air Compressor filter, just a bit of plastic and foam.
The Air Compressor with makeshift foam filter – this had almost disappeared down the air intake tube. it is fine now, seems very good in fact and a lot smaller and quieter than I was expecting..
The first sounds of chuff chuff were just brilliant, like it was coming to life, a completely amazing feeling that I don’t think I will forget. I was right in saying that for me just to get it made, assembled and having learnt so much in doing it would have been enough for this 1st project – to have it running as well is just superb. I will be drinking a toast to the little engine tonight, maybe one or two of you will join me..
The link for the video is here **LINK** – apologies for the quality again, I need to look at upgrading my iphone before starting the Stuart no. 1, and please excuse the location, it was done in an old out house (no dust)..
Have a good weekend everyone and as I said before a big big thanks to everyone…
Cheers.
Allan.
ps. I'm going to miss posting on this little thread…been great fun.
Edited By Allan. on 14/03/2014 13:31:14