Oh Dear- poor Juliet seems to have had a rather hard life before you rescued her!
Whoever made that boiler seems to have struggled to do so, too, as there is nearly as much silver-solder lost over the surface as there should be in the joints. Some shows signs of over-long heating, too. However, all that wasted solder is not a structural or functional fault – just an expensive mess. More worrying to me is the battered state of the regulator-rod gland and the valve near it; and I hope it’s only an optical illusion that makes the end of the rod look bent. Errr, why is the metal around the fire-hole and the stay-head grey?
Anyway, back to the immediate question……
It does seem built-up scale is the fault so I’ll assume so……
Thank you Nick for posting the drawing.
My caution would be, dismantle only as necessary but since we’ve now established the backhead gland is no longer a problem apart from the broken screws, the dome will need removing as you’ve started.
Use descaler first to remove as much external crud as you can, including around those dome studs. Some of more greenish stuff on the whole thing might actually be residual silver-soldering flux, or copper salts from it having remained on there.
You don’t want oil inside the boiler if you can help it, but the dome flange might need some help with penetrating-oil. Before trying that though, try more descaler. Citric acid solution or proprietary kettle descaler is effective without risking it lunching on the metal too much.
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If really necessary, and this is not something I would try lightly for the obvious reason we’ve already seen, you could try removing the dome studs, aiming for just alternate ones first. Mark the dome and bush flanges for re-assembly orientation, if not already marked, as we can’t guarantee it has sufficient angular accuracy for easy fitting.
To remove and refit these studs, use a proper stud-box or the locked-nuts method, and again, let them slumber in penetrating-oil first.
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Now, once the regulator is exposed, and probably seen as coated in scale, use the descaler again to clean it as well as possible before trying to move or dismantle anything.
Examining Nick’s drawing, the steam circuit looks very frail as designed. It’s unlikely anyone now would screw that header mounting straight into the tube-plate, or the backhead flange into the backhead, as the drawing specifies, although your example looks as if it does have a separate mounting silver-soldered in place.
So I’d be wary of trying to dismantle that wet header. We don’t want any washing-out water in the cylinders, but the boiler is off the locomotive anyway, so push some hose onto the superheater outlet to drain into a suitable receptacle.
Now refit the backhead gland, at least for the time being, enough to support gently trying to operate the regulator as the valve frees off.
This done, feed some descaler solution down that vertical inlet, and let it work. Tip it out – it won’t hurt ending up inside the boiler – give it another dose. Using hot water will speed the reaction somewhat, but give it plenty of time.
Empty that, rinse with distilled / fridge-defrosting / filtered rain – water. Carefully try operating the valve. Of course, if that was already open, the descaler solution will be in the superheater or drain – but if this locomotive suffered much priming, the superheater will likely be partly scaled-up too. Raise the end of the tube to keep the descaler in place.
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So the whole approach then is to try to cure the problem without taking too much apart, and especially if at all possible, without disturbing those very fragile pipework threads. Let’s hope we don’t need get that far!
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While at it, remove and descale the external fittings, and when replacing them, use copper shim washers for orientation and sealing. The latter may be helped by a thin smear of non-hardening jointing compound on the thread, but don’t use PTFE tape. That can shed slivers capable of blocking gauge-frame water-ways, or preventing clack-valves closing properly.