So the air bearing on a taper spindle really is a fail. Plan B, is to make an air bearing headstock for a sieg6 lathe bed that I have. Convert the carriage to be on linear rails, and make it specifically for finish only and light duty things. The new spindle will be a parallel one and will look into the carbon air bearing pads like Dan Gilbert did making it adjustable for the loads etc. I just need to learn a lot more about air bearings for sure.
Made a replacement bronze bush for the S7 and recut the 12deg,25 mins (12.4166 deg) inclusive taper on the spindle matching the bush. The bush needs to be scraped and fitted to the shaft after it is pressed into the housing.
I did not have that much success with the taper roller bearings. They worked, but there is a coupling happening from the slight error of the bearings concentricity and the concentricity of the shaft to the shaft taper. It may have been that they were not the high precision taper roller bearings.
Switched back to the angular contact bearings and it was better but not where I wanted it.
Hence the reason for the re cutting of the shaft taper and making sure it was concentric to the existing diameters of where the bearings sit and the chuck register diameter. It was very close just over 0.01 mm TIR
The new coated carbide cut the taper very well at around 400 rpm or so.