I’ve resolved the wobble now, but still don’t understand what I did wrong in the initial machining.
The process I followed was this –
1. Set Flywheel casting (7 inch diameter) on the faceplate to run true (as possib le) against the flywheel areas that will remain unmachined.
2. Skimmed the front edges of the flywheel and the top surface, bored the hub as a series of ops without changing the setup.
3. Turned the flywheel over and set to truth using a DTI on the machined surfaces (1/10 clock).
4. Machined remaining front surface
5. Flywheel wobbles on the crankshaft.
I could understand if the final machined surface didn’t run true, but the whole flywheel had a clear wobble. This process should be fool proof (or Muddle Engineer proof!) shouldn’t it?
As above, I’ve sorted the thing, but don’t understand why the wheel wasn’t right first time.
Regards
Steve