Posted by Ro on 11/07/2020 15:26:30:…
…I made up a quick top hat and trued the jaws with a carbide boring bar and the top hat held in the back of the jaws (then reversed the top hat to the front and did the same for the very rear of them).
The jaws now grip fully along the length and don’t slip at all!
I was slightly worried about the work on the scroll affecting the runout, but after testing at multiple diameters I seem to be getting a maximum of about 3 thou.
Possibly because when you held the top hat ring in the rear of the jaws and tightened the jaws inwards, the front tips of the jaws were pushed inwards, the opposite of the way they are pushed when in use holding a piece of round bar etc.
That is why the clover leaf plate I posted above works better. It pushes the front tips of the jaws outwards while they are being machined, replicating the position they are in during normal operation.
If there is a bit of slack between the jaws and the slots in the chuck body they run in, it can make quite a difference.
I got the chuck on my 1937 lathe to run within one thou using this method.
Edited By Hopper on 12/07/2020 02:43:19